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Elimination of low-frequency unstable combustion phenomenon of a certain engine(PDF)

《火箭推进》[ISSN:1672-9374/CN:CN 61-1436/V]

Issue:
2011年06期
Page:
26-29
Research Field:
研究与设计
Publishing date:

Info

Title:
Elimination of low-frequency unstable combustion phenomenon of a certain engine
Author(s):
CHEN Zhan HE Wei-tao WANG Ke-li
Xi’an Aerospace Propulsion Institute, Xi’an 710100, China
Keywords:
low-frequency unstable combustion failure mode failure elimination
PACS:
V434-34
DOI:
-
Abstract:
The failure mode of an engine is analyzed and the model of a corresponding part is established in this paper based on the phenomenon of low-frequency combustion instability occurred in hot fire testing of the engine. The phenomenon of the low-frequency unstable combustion was eliminated after the design improvement of a corresponding part.

References:

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[2]HARVEY D W. Throttling venturi valves for liquid rocket engines, AIAA 70-703 [R]. USA: AIAA, 2003.
[3]TRW. 500Hz pressure oscillations on LMDE, TRW 01827-6221-TO-00 [R]. [S. l.]: TRW, 1969.
[4]朱宁昌. 液体火箭发动机原理[M]. 北京: 宇航出版社, 1994.

Memo

Memo:
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Last Update: 1900-01-01