|Table of Contents|

Investigation on reason of overheating of turbine housing in liquid rocket engine(PDF)

《火箭推进》[ISSN:1672-9374/CN:CN 61-1436/V]

Issue:
2013年02期
Page:
35-39
Research Field:
研究与设计
Publishing date:

Info

Title:
Investigation on reason of overheating of turbine housing in liquid rocket engine
Author(s):
ZHANG Zhong-li ZHANG Meng-zheng LI Fu-yun
Xi’an Aerospace Propulsion Institute, Xi’an 710100, China
Keywords:
-
PACS:
V434.2-34
DOI:
-
Abstract:
The temperature variation of gas-generator exhausting shell and turbine's inlet-outlet housing are analyzed during No. 001~003 hot test of liquid rocket engine (LRE). With unsteady heat transfer methods, the temperature variation of turbine housing caused by the gas-generator working at different flow rate and efficient in the 003 time hot test were simulated. The simulation result shows that the overheating of turbine housing is because of too much high efficiency of gas-generator.

References:

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[2]张金容, 靳爱国, 汪亮. 泵压式液体火箭发动机变推力方案选择[J]. 航空动力学报, 2008, 23(5): 921-926.
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[4]张忠利. 高空滑行期间氧化剂泵壳体冷却方案研究[J]. 火箭推进, 2004, 30(5): 22-27.
[5]张忠利. 液体火箭发动机自引射工作过程传热研究[J]. 火箭推进, 2012, 38(1): 31-36.

Memo

Memo:
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Last Update: 1900-01-01