PDF下载 分享
[1]来代初,苏红军,李伟.液氧/煤油发动机煤油高低温试验工艺技术[J].火箭推进,2009,35(04):53-58.
 Lai Daichu,Su Hongjun,Li Wei.High and low temperature test technology of kerosene of the LOX/kerosene engine[J].Journal of Rocket Propulsion,2009,35(04):53-58.
点击复制

液氧/煤油发动机煤油高低温试验工艺技术

参考文献/References:

[l]马瀚英.航天煤油[M].北京:中国宇航出版社.2003.
[2]来代初,唐德芳.RD一120发动机试车台[J].火箭推进, 2002,28(5):31—34.
[3]郭霄峰.液体火箭发动机试验[M].北京:宇航出版社. 1990.
[4]徐烈,朱卫东,汤晓荧.低温绝热与贮运技术[M].北 京:机械工业出版社.1999.
[5]QJ3277-2006液氧煤油发动机试验方法[S].
[6]GJB5425-2005液体火箭发动机用煤油规跚[s].

相似文献/References:

[1]秦永涛,宋 阳,苏红芳,等.火箭发动机试验管道多余物人机环境控制方法[J].火箭推进,2015,41(06):80.
 QIN Yongtao,SONG Yang,SU Hongfang,et al.Method of man-machine-environment control over foreign object debris in pipelines used in rocket engine test[J].Journal of Rocket Propulsion,2015,41(04):80.
[2]黄其殷,王幸果,刘 上,等.液氧/煤油发动机起动箱仿真与试验研究[J].火箭推进,2015,41(03):21.
 HUANG Qi-yin,WANG Xing-guo,LIU Shang,et al.Simulation and test study on starting box of LOX/kerosene rocket engine[J].Journal of Rocket Propulsion,2015,41(04):21.
[3]董 冬,张少博,刘 晓.试验状态信息管理软件设计[J].火箭推进,2013,39(06):72.
 DONG Dong,ZHANG Shao-bo,LIU Xiao.Design of information management software for test status[J].Journal of Rocket Propulsion,2013,39(04):72.
[4]李 程,刘站国,徐浩海.双推力室起动同步性研究[J].火箭推进,2014,40(04):16.
 LI Cheng,LIU Zhan-guo,XU Hao-hai.Study on synchronous ignition of dual-thrust chamber engine[J].Journal of Rocket Propulsion,2014,40(04):16.
[5]王军钢,赵万明,唐丽萍.提高低温压力测量准确度的方法初探[J].火箭推进,2012,38(05):65.
 WANG Jun-gang,ZHAO Wan-ming,TANG Li-ping.Discussion on method of improving accuracy of pressure measurement in low temperature[J].Journal of Rocket Propulsion,2012,38(04):65.
[6]姬俊锋,吴光中,马利亚,等.液体推进剂发动机试验多工况流量控制方法[J].火箭推进,2011,37(02):71.
 JI Jun-feng,WU Guang-zhong,MA Li-ya,et al.Multiple-working-conditions flowrate control for liquid engine test[J].Journal of Rocket Propulsion,2011,37(04):71.
[7]李建军,薛宁.液氧平均流量测量研究[J].火箭推进,2010,36(01):67.
 Jianjun,Xue Ning.Research on measurement of LOX mean flow rate[J].Journal of Rocket Propulsion,2010,36(04):67.
[8]赵万明,王军钢.液体火箭发动机试验负推力修正[J].火箭推进,2010,36(06):56.
 ZHAO Wan-ming,WANG Jun-gang.Correction of negative thrust in liquid rocket engine tests[J].Journal of Rocket Propulsion,2010,36(04):56.
[9]曹文庆,谭海林,李伟.低温发动机试验推进剂人口温度控制[J].火箭推进,2009,35(03):52.
 Cao Wenqing,Tan Hailin,Li Wei.Propellant inlet temperature control for cryogenic rocket engine tests[J].Journal of Rocket Propulsion,2009,35(04):52.
[10]李向阳,王晓锋,宣统,等.液氧/煤油发动机煤油预压涡轮泵技术[J].火箭推进,2009,35(01):16.
 Li Xiangyang,Wang Xiaofeng,Xuan Tong,et al.Techniques of kerosene booster turbopump for LOX/kerosene staged combustion cycle engine[J].Journal of Rocket Propulsion,2009,35(04):16.

备注/Memo

收稿日期:2009--06—13;修回日期:2009-07—18。 作者简介:来代初(1955一),男,研究员。研究领域为液体火箭发动机试验。

更新日期/Last Update: 1900-01-01